Author
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Topic: novi 2000
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Dubc
New Member
Member # 5466
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posted
my buddy and I put on a novi 2000 yesterday on his 2000 gt...started it up...without being tuned and sounding like shit...it seems that its always in boost but it shouldn't be unless there is a load...gauge is reading 1-2 lbs boost off idle....we tried to mess with the blow off but that didn't do didly...anyone have advice?
Posts: 3 | From: Bay Area | Registered: Mar 2005
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2stangs69-91
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Member # 1951
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posted
It should have a bypass valve not a blow off. It might be stuck Does it have a vacuum line going to the bypass valve?
-------------------- 69 Mustang on hold 1991 LX hatch getting a make over 1994 F150 4X4 351 2006 Yamaha V-max 1200 Modded
Posts: 3711 | From: Redding | Registered: Oct 2002
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MINGRYGT
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Member # 2439
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posted
Maybe you just have a bad gauge.
-------------------- R.I.P. MIKE STARKEY 5-17-03
Posts: 488 | From: Concord | Registered: Feb 2003
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94gt
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Member # 3060
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posted
did you route the bypass valve into the discharge tube? and where do you have to guages' press line coming from?
-------------------- 2020 Explorer ST 2011 Silver Raptor 'Screw
Posts: 5777 | From: Beavercreek, OH | Registered: Jul 2003
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andyman_2k01
CAFords OG
Member # 1448
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posted
it's on my 00gt. We found out that the piping we fabricated that connected the bypass valve to the power pipe had torn apart. unmetered air made it run real rich. we rewelded the power pipe to get a new hose on that would connect the two (bypass and power pipe) and the car seemed like it ran fine for about 20 seconds. Now the car is bouncing back and forth from 1000 rpm to 500 rpm continously. anyone know what this could be from? maybe i have another air leak somewhere? oh and it's a Vortech Mondo Bypass Valve and a 4" powerpipe.
-------------------- -00 Mustang GT (R Clone) -99 Saleen Convert. #231-SOLD
Posts: 1503 | From: Bay Area, CA | Registered: Jun 2002
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