Author
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Topic: Well, I just finished pulling the heads off of the 'vert
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TheBrain
I'm the Real John Force
Member # 35
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posted
AND ALL I DID WAS BLOW BOTH HEAD GASKETS !!!!!!!! WOOHOO !!!!!!!!!! Looks like about $100 in gaskets and I will be back on the road
The pistons still look GREAT Guess JE pistons don't suck as much as that cock smoker @ Force Fed Performance told me when the same thing happened to my car on his dyno awhile back The heads were undamaged this time. Last time I had to milled the heads about .020 since it burned the head between cylinders.
I am a happy happy guy right now !!!!!!
Just thought I would keep you guys updated
Brian
-------------------- 1989 LX vert 342 11.662 @ 116.65 1.57 60ft. N/A 10.227 @ 134.59 1.41 60ft 200 shot 3600lbs 2003 Ranger 4 door 15.99 @ 87
Posts: 1264 | From: Back in Redding CA | Registered: Jul 2000
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sac 5.0
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Member # 2980
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posted
sounds great happy for you lots better then spending money on a new car or a motor like you were talking about.hope you dont run into another lean condition again
Posts: 1021 | From: sac | Registered: Jun 2003
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DropTopFox
drama
Member # 1689
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posted
quote: Originally posted by TheBrain: AND ALL I DID WAS BLOW BOTH HEAD GASKETS !!!!!!!! WOOHOO !!!!!!!!!! Looks like about $100 in gaskets and I will be back on the road
The pistons still look GREAT Guess JE pistons don't suck as much as that cock smoker @ Force Fed Performance told me when the same thing happened to my car on his dyno awhile back The heads were undamaged this time. Last time I had to milled the heads about .020 since it burned the head between cylinders.
I am a happy happy guy right now !!!!!!
Just thought I would keep you guys updated
Brian
Was your car dyno tuned on the 200 shot. And let me get this straight so just the head gaskets blew right, no head or piston damage
-------------------- Go out and do something for yourself today everyone, quit depending on others
-Me http://www.CaliforniaFords.com/cgi-bin/album.pl?album=00001689
Posts: 4003 | From: San Bruno | Registered: Aug 2002
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TheBrain
I'm the Real John Force
Member # 35
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posted
No dyno tuning on the car at all No piston or cylinder head damage
I will come clean on what caused the problem: OPERATOR ERROR
Kinda forgot that I had straight 91 octane gas and not the 98-100 octane I run when on the bottle
So kids, today's lesson is Don't hit a 200 shot on pump gas
Brian [ January 18, 2004, 05:55 PM: Message edited by: TheBrain ]
-------------------- 1989 LX vert 342 11.662 @ 116.65 1.57 60ft. N/A 10.227 @ 134.59 1.41 60ft 200 shot 3600lbs 2003 Ranger 4 door 15.99 @ 87
Posts: 1264 | From: Back in Redding CA | Registered: Jul 2000
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FasterDamnit
Bad Attitude
Member # 442
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posted
So- will we see a resurrection of the vert? Still gonna try for the 10 second run on bot tle?
Posts: 2971 | From: NorCal | Registered: Sep 2001
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MR GO FAST
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Member # 2088
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posted
quote: Originally posted by TheBrain: So kids, today's lesson is Don't hit a 200 shot on pump gas
Brian
Let me know when you go to the track.
-------------------- 1986 Gt that is faster than FOSTANGS pinto
Posts: 3729 | From: ATWATER/SANJO/RWC | Registered: Nov 2002
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98slowhoe 'FIFTYLX'
Uncle Frank
Member # 895
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posted
quote: Originally posted by TheBrain:
So kids, today's lesson is Don't hit a 200 shot on pump gas
Brian
Let me put that in my palm pilot
-------------------- AKA Franky Freaking 5 liter
Advanced Engine Development SCT dealer Dynotuning Engine building 916*275*8212
88 4runner on 42's
Posts: 4206 | From: Folsom | Registered: Feb 2002
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TheBrain
I'm the Real John Force
Member # 35
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posted
quote: Originally posted by FasterDamnit: So- will we see a resurrection of the vert? Still gonna try for the 10 second run on bot tle?
Resurrection will occur next weekend. I am NOT going to try to run 10's on the bottle, I WILL run 10's on the bottle Let's just hope they can get the track prepped properly so I don't die !!!!
quote: Originally posted by MR GO FAST: Let me know when you go to the track.
Will do, should be in a couple weeks [ January 18, 2004, 06:38 PM: Message edited by: TheBrain ]
-------------------- 1989 LX vert 342 11.662 @ 116.65 1.57 60ft. N/A 10.227 @ 134.59 1.41 60ft 200 shot 3600lbs 2003 Ranger 4 door 15.99 @ 87
Posts: 1264 | From: Back in Redding CA | Registered: Jul 2000
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Yellow94GT
Mr. 60 FT
Member # 431
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posted
Glad to hear that the real John Force will have something to race again
-------------------- AED
1994 GT Bucket that will likely never run 1999 SLOLEEN Twin Turbo Coyote 2008 F250 580 RWHP 1129 RWTQ
Posts: 5990 | From: Cameron Park, Ca | Registered: Sep 2001
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jmcclesk
Moderator
Member # 1355
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posted
Oh Yea!!!
-------------------- Ford trained ASE master tech.
Posts: 4024 | From: marrysville | Registered: May 2002
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season'd 88
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Member # 169
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posted
I guess this means we dont get broken parts pictures.. good to hear though.
Posts: 1383 | Registered: Feb 2001
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FordPny
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Member # 510
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posted
quote: Originally posted by TheBrain: So kids, today's lesson is Don't hit a 200 shot on pump gas
That should be a new bumper sticker
Glad everything is ok
-------------------- Holla at yoo boooyyy
Posts: 2458 | From: San Jose CA | Registered: Oct 2001
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2000BlackGT
Loyalty
Member # 283
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posted
quote: Originally posted by Yellow94GT: Glad to hear that the real John Force will have something to race again
lol hope to see you out there again Brain
Posts: 2833 | From: Chico, CA | Registered: Jun 2001
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Camara90
1%
Member # 134
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posted
man that sucks i thought you wanted a reason to build A DART BLOCK!! J/K
MAKE SURE YOU GET YOURSELF SOME GOOD GASKETS THIS TIME!
-------------------- 92GT,stock short block,9:1 TFS 170's,perf rpm,custom cam,1 5/8 shorties,C4 trans. std. 356hp, 350tq 11.85@111.9mph on motor.
Posts: 2351 | From: 707 | Registered: Jan 2001
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Blue Oval
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Member # 2548
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posted
AWESOME! i seruiosly thought u messed it up big time when i read the story.Hope to see u run that 10.
-------------------- 65 Coupe 306, AFR's 89 Cali. Ed. Saleen "sold" BAB 89 GT 08 Yamaha R6
Posts: 2345 | From: Sacramento | Registered: Mar 2003
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TheBrain
I'm the Real John Force
Member # 35
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posted
quote: Originally posted by Camara90: man that sucks i thought you wanted a reason to build A DART BLOCK!! J/K
I do want a reason to build a Dart block !!!!!!! However I would much rather built it because I want to not because my motor is blown and I HAVE to !!! ROFL
Should be back at the track on the 31st
Brian
-------------------- 1989 LX vert 342 11.662 @ 116.65 1.57 60ft. N/A 10.227 @ 134.59 1.41 60ft 200 shot 3600lbs 2003 Ranger 4 door 15.99 @ 87
Posts: 1264 | From: Back in Redding CA | Registered: Jul 2000
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ForceFedPerformance
New Member
Member # 2423
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posted
[ November 12, 2004, 06:41 PM: Message edited by: ForceFedPerformance ]
Posts: 5 | From: Sacramento,Ca. | Registered: Feb 2003
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2stangs69-91
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Member # 1951
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posted
BTW I was standing right there when this all happened. The first thing you said was the piston had a hole in it. Brian replied to you that he had the good J&E pistons to which you said "they are Junk" You were very rude when this all happened. I have a Vortech blown car that needs to be on a Dyno and I wouldn't use you after that. BTW the last post on this is almost a Year old why dig it back up? You had plenty of time to square this all up over the last 2 years. [ November 12, 2004, 11:07 AM: Message edited by: 2stangs69-91 ]
-------------------- 69 Mustang on hold 1991 LX hatch getting a make over 1994 F150 4X4 351 2006 Yamaha V-max 1200 Modded
Posts: 3711 | From: Redding | Registered: Oct 2002
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2stangs69-91
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Member # 1951
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posted
Hmmmm I guess Mr Force Fed didn't like what I had to say LOL
-------------------- 69 Mustang on hold 1991 LX hatch getting a make over 1994 F150 4X4 351 2006 Yamaha V-max 1200 Modded
Posts: 3711 | From: Redding | Registered: Oct 2002
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hidnn.o.s.
¯
Member # 1219
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posted
wish someone could have quoted him so we could see
-------------------- R.I.P. Willie G. You are missed on this forum
Posts: 15950 | Registered: Apr 2002
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bunchmyfunky
CAFords Drag Racing Mod
Member # 360
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posted
quote: Originally posted by hidnn.o.s.: wish someone could have quoted him so we could see
It was a poor attempt at an excuse that made no sense.
Posts: 2433 | From: Vacaville | Registered: Jul 2001
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Yellow94GT
Mr. 60 FT
Member # 431
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posted
quote: Originally posted by 2stangs69-91: Hmmmm I guess Mr Force Fed didn't like what I had to say LOL
Yeah, nice of him to edit his post like that
-------------------- AED
1994 GT Bucket that will likely never run 1999 SLOLEEN Twin Turbo Coyote 2008 F250 580 RWHP 1129 RWTQ
Posts: 5990 | From: Cameron Park, Ca | Registered: Sep 2001
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TheBrain
I'm the Real John Force
Member # 35
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posted
Still not sure why he felt the need to bring all of this back up
Brian
-------------------- 1989 LX vert 342 11.662 @ 116.65 1.57 60ft. N/A 10.227 @ 134.59 1.41 60ft 200 shot 3600lbs 2003 Ranger 4 door 15.99 @ 87
Posts: 1264 | From: Back in Redding CA | Registered: Jul 2000
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v-town coupe
fordologist
Member # 2771
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posted
glad t see ur still alive brian! you'll bee john forc'n it in no time!
Posts: 4597 | From: the V-town | Registered: May 2003
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